You reckon? It looks to me like it flew right until the point that it stuck the ground. And then probably dthe battery fell out because of the impact.
@flat-earther4 ай бұрын
do you not have altitude OSD element?
@wtb5674 ай бұрын
I probably do. I should probably add it.
@etalon31414 ай бұрын
GPS altitude is notoriously unreliable, where the drone activated its GPS RTH was at a lower elevation. My guess is the drone thought/was flying level towards you, but the ground basically rose to meet it. Increasing the GPS rth altitude will help.
@wtb5673 ай бұрын
I tried this same Flywoo quad on INAV 7.1 now and its return to home and navigation hold works perfectly. But I am having lots of strange behavior on Betaflight GPS rescue with the same quad. That said.... GPS rescue now works perfectly on my other bigger 5 inch Nazgul quad. Its just on the Flywoo that it gives problems.