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DIY Arduino based Toroid coil winding Machine | Arduino project

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Mr Innovative

Mr Innovative

Күн бұрын

$2/5pcs 2Layer & $5/5pcs 4Layer PCBs: jlcpcb.com
Hello friends In this video I have made a toroid coil winding machine using arduino as controller,
This machine is automatically winding the turns and also rotate toroid core automatically.
For user input and interaction I have used a rotary encoder and 16x2 LCD display.
User can enter data like diameter of toroid core, number of turns and how much area of toroid core need to wind.
I have program it in a way so it can be used for variety tor ID/OD toroid cores just enter the core OD and do some mechanical adjustment.
Currently this machine giving just ok ok result but I want it to upgrade further so it can be practically useful, please give your suggestions and ideas in comment box because I am not familiar with toroid coil winding machine, I have never seen in it live in my whole life. I made this project by just watching video on net. so I might be not completely aware about its working process.
All details like code, circuit, item list, construction details etc are available on my website.
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Rotary tool :- amzn.to/2FM3Lnh This video is made for entertainment purposes only. Please use judgment, care, and precaution if you plan to replicate. WhatsApp for custom projects +91 7600079068

Пікірлер: 761
@JoseSilveira-newhandleforYT
@JoseSilveira-newhandleforYT 4 жыл бұрын
I'm genuinely impressed that you actually made a perfectly working toroidal core winder! The inaccuracies you are getting result from the wood construction and a less effective wire guiding system, but the concept is there and is perfect! Well done! You can use printer pickup rollers for driving and guiding the toroid (with plastic washers to form flanges). In fact, you can disassemble an old inkjet printer (you probably can get it for free) and salvage most of the parts required (depending on the printer model: belts, rollers, optical sensors, stepper and drive motors, plus assorted hardware that may become handy in construction), to get yourself a winding machine that will cost you mainly the hours spent building it. Finally, I must congratulate you for making all the information freely available - it's relatively easy to find used toroidal transformers in scrapyards, that can be rewound to meet to personal needs - normally the primary can be used as it is (assuming primary is OK) and the secondary (outer windings) can be taken out and rewound with your machine. I suggest winding experimental 10 turns secondary and measure the voltage obtained, to get the volts per turn ratio (voltage measured divided by ten, normally much less than 1). If you need more accuracy, wind 100 turns, measure and divide by 100 and then multiply by the desired voltage to get the corresponding number of turns, not forgetting the wire gauge must be enough to handle the current (that depends also on the power the core can provide). I believe there are a lot of capable young people that would benefit from this - Transformers are expensive (shipping is expensive too, due to weight). Even a burnt transformer can be salvaged, because the core is normally OK, but then you need to wind both primary and secondary(ies). To calculate primary and secondary turns from scratch, I suggest a very good tutorial from Ampletos (kzfaq.info/get/bejne/h5x3nrZ_y6epqGg.html). It's in Spanish, but if you turn CC on, you can have subtitles in your language - technical information is normally understandable, even if YT translation gets a bit awkward. Long post, in the hope that this may help any enthusiasts out there :-)
@MrInnovative
@MrInnovative 4 жыл бұрын
Thanks man for guidance 👍 really helpful
@JoseSilveira-newhandleforYT
@JoseSilveira-newhandleforYT 4 жыл бұрын
@@MrInnovative I'm glad you liked it! Your project deserves attention from young enthusiasts and the reuse of old printers and transformer cores is the way to go - recycling is the last resort!
@seanjackson5527
@seanjackson5527 4 жыл бұрын
Ampletos's video is by far the most clear I've seen.
@enilenis
@enilenis 4 жыл бұрын
I built an entire CNC-like woodburning machine entirely out of parts found in a photocopier. Steppers, rollers, gears - that thing had entire assembly. I have a video somewhere on my channel. Best part, there is a ton of office equipment that gets discarded as trash. They are a great source of parts for makeshift automation.
@alexstone691
@alexstone691 3 жыл бұрын
Where would you find a toroidal transformer at scrapyards? I need some but nobody sells the cores and the wound ones are really expensive
@Enigma758
@Enigma758 4 жыл бұрын
I don't care that people are saying that it could be better, that's true of anything. The fact that you made a working toroid coil winder is impressive in and of itself.
@WistrelChianti
@WistrelChianti 4 жыл бұрын
It's super impressive work! Something I wonder might help: Currently the wire comes from anywhere on the spool (depending on position of the unravel) to the toroid and this might be causing an innaccuracy in position. I'm thinking if you added a little guide ring in front of the spool (between the spool and the toroid) and thread the wire through it before attaching to the toroid, the wire will always be coming from the same spot. The distance between the spot the toroid will always be the same. I'm not basing this idea on anything more scientific than a vague recollection of a sewing machine feeding mechanism though. :D
@MrInnovative
@MrInnovative 4 жыл бұрын
really thanks for your guide....
@the_eminent_Joshua_E_Hrouda
@the_eminent_Joshua_E_Hrouda 4 жыл бұрын
Yeah, that's probably what caused most of the variability in the turns spacing
@conorstewart2214
@conorstewart2214 Жыл бұрын
I was just thinking of a sewing machine when reading the first half of your comment, it is very very common to use a guide when dealing with anything on spools, even like fishing rods that take the line coming in and run it through a reciprocating guide to make sure it winds up neatly and evenly and without tangles.
@skeletor8250
@skeletor8250 3 жыл бұрын
This is a lot of work. This man had to do a lot of hands-on basic experimentation work, a lot of design work, a lot of re-design and refinement work, then a lot of work to make it instructional to others, and a lot of work of filming and post-production to make it easy to follow. I do not see a lot of women doing this kind of stuff. Hats off to his intellect and perseverance.
@goldnoob6191
@goldnoob6191 4 жыл бұрын
You should replace the DC motor with another stepper, the winding would be much more precise. Anyway this is a smart idea.
@nixxonnor
@nixxonnor 4 жыл бұрын
Why do you need another stepper motor when you have the revolution counter? The problem seemed to be the jerky feeding of the toroid.
@AnalogDude_
@AnalogDude_ 4 жыл бұрын
@@nixxonnor because you have 24 steps per revolution.
@theman3282
@theman3282 4 жыл бұрын
this construction/design is commonly found in Chinese made coil winder.
@recer_
@recer_ 4 жыл бұрын
@@nixxonnor at 1:06 - 1:07 it appears to have skipped a tick.
@DavidKristiawan
@DavidKristiawan 4 жыл бұрын
@@recer_ but the winding count increases even though the led isn't on at that time. I think this is because the camera shutter isn't synchronized with the rotation.
@KeithOlson
@KeithOlson 4 жыл бұрын
That is a *VERY* useful build. For more placement accuracy, I suggest using a swinging arm that is anchored by the spool, with the wire going through an eyelet at the end, positioned as close to the toroid as possible without running into it.
@mfratus2001
@mfratus2001 2 жыл бұрын
Thank you for showing us this! I watched a video about winding toroids but apparently only half-understood it. Thanks for making this great project!
@Andospar
@Andospar 3 жыл бұрын
Magnificent!!! Innovative and nicely done. You asked if there were any suggestions for improvements and the only thing I could see was the need for a feed spool tensioner. But with this comment being a year after posting, Your keen insight has probably already addressed this. 👍
@TopCat2021
@TopCat2021 4 жыл бұрын
I'm not sure how you would improve the machine but what you have created is VERY impressive, great job Sir!
@suelynch
@suelynch 4 жыл бұрын
Between 1978 to 1990 I worked for a company that made Toroids. We made them G.R.O.S.S. and Mu-metal. We also manufactured C cores, E cores and distributor gap.
@shovington67
@shovington67 4 жыл бұрын
Regardless of the initial outcome, it's still a proof of concept that actually worked even though you used fairly primative parts and pieces scavenged from other unrelated devices. With some further investment of time and energy, this coil winder will be an intricate part of a much larger apparatus, that will contribute to the building of all kinds of much needed equipment. Well done ! You have an exceptional ability to visualize in 3 dimensions.
@MrInnovative
@MrInnovative 4 жыл бұрын
thank you...
@davidlarson2534
@davidlarson2534 2 жыл бұрын
Add a DTMF keyboard to input the numbers. It will simplify operation. Keep the rotary switch to access various modes, speed, pause, etc.
@scaletownmodels
@scaletownmodels 4 жыл бұрын
It's a very nice build. I like it. I don't really see anything particularly wrong with it at this stage, just needs refining of individual elements like others have said. Improve the tracking of the moving parts, add in some better wire guidance. Personally I would probably 3d print an outer gear ring to replace the belt drive and have it engage a stepper for precise control and no slipping, but that's just me. I do like how on commercial models, the large drive ring is itself a giant spool that you prefill with enough wire to do the job.
@vandanamittal5754
@vandanamittal5754 Жыл бұрын
This is very appreciable. Although there is always a scope of improvement as per available comments.The PCB shown is the only outsourced requirement, rest is self manageable.Also for thick wire size like swg12/13/14 we have to take the necessary measures of the parts. Again a very very useful successful attempt. All the very best.
@ctbully
@ctbully 4 жыл бұрын
This really excellent work. If you were winding a toroidal transformer you would need to have automatic adjustment of the turning mechanism for the toroid as the thickness of the coil increases
@H3xx99
@H3xx99 3 жыл бұрын
For the toroidal core holder, I would have used a solution like the one you used for the main drive wheel, but with spring loaded gripping arms. I would use a spring on the drive wheel also, instead of a wing nut. As for the control system, I'd probably go with a raspberry pi instead of arduino, but that's purely personal preference. I love the simplicity of the interface. I'd probably try to add a linear coil winder also. Maybe using a linear screw to move the coil and wind smoothly.
@conorstewart2214
@conorstewart2214 Жыл бұрын
An arduino is much much more suitable here than a raspberry pi. Why would you need a pi for this? What benefits would it bring? This is something that needs precise timing and not much processing, essentially the opposite of what you get with a pi, lots of processing power and not a real time system. So microcontrollers are much more suitable for this application.
@KholyScript
@KholyScript 3 жыл бұрын
Well, at the first glance, you need basic improvements that will make the coil more consistent. First you need to count half cycles so every side of the coil should have its own displacement. The inner side of the coil should have a min displacement of the wire diameter and this will guarantee that the wire will not overlap, then the outer displacement should be calculated using the the ratio of the outer diameter to the inner diameter of the coil multiplied by the displacement you set for the inner side. Then you should make some minor modifications in the way you calculate the displacement. You should get another stepper with the highest possible step count, that will give you more accuracy if you counted quarter steps or even less. Then you calculate the displacement for each step or quarter step using the inner diameter of the coil. That will give you a seamlessly consistent and homogeneous coil. It's also good to start the first round at the inner part of the coil and always use that position as the starting position to get accurate changes with each iteration. Last, try to start the DC motor with a slow speed, then you can keep the speedometer controlling the speed while it's rolling untill you can determine the maximum stable speed of rolling. Keep in mind that the optimal speed will ever change whenever you've changed the coil's diameter. Have fun dude 😎👏
@albratgaming2348
@albratgaming2348 3 жыл бұрын
Only suggestion I would make is to put some sort of tensioner on the wire coming from the coil... This will improve the winding by double. As it looked like there may have been slack wire winding that allowed it to drift sideways. Othwise a nice looking and well working machine !!
@ottotater2787
@ottotater2787 Жыл бұрын
This isn't just cool, this is leading towards JoeBob homie being able to invent their own electronic components at home instead of only in big fancy lab factories. This opens the door for more overlooked geniuses to be able to do their stuff.
@GaryMcKinnonUFO
@GaryMcKinnonUFO 3 жыл бұрын
Superlative work :) Being a long time coiler i can appreciate the thought, effort and time that went into designing and testing this lovely device. Liked and subbed.
@valterbaldideoliveira6609
@valterbaldideoliveira6609 3 жыл бұрын
CR
@InsideOfMyOwnMind
@InsideOfMyOwnMind 4 жыл бұрын
Part of the time the core rollers are on windings and part of the time not leading to uneven winding. Possibly more rollors would help or a way to accurately monitor the degrees of rotation. Right now it's open loop.
@thatshowtheyare9227
@thatshowtheyare9227 2 жыл бұрын
Somebody need to give this man a million dollar so the next project can become reality
@conorstewart2214
@conorstewart2214 Жыл бұрын
It looks like you could do with some tension on the spool of wire, in the video it seems like it is wrapped round the coil pretty loosely. I think you maybe tried that with the spring, but some friction on the spool should be enough, also a wire guide is probably necessary to keep the spacing even.
@HyperspacePirate
@HyperspacePirate 2 жыл бұрын
this is one of my favorite channels on youtube
@kschabowski
@kschabowski 3 жыл бұрын
I'm really impressed by your work!!! For a device that has lots of manually created elements (by manually I also mean elements that you made with a lathe but not an automatic lathe) it works really smothly. Of course there are some things to fix to make it more reliable and consistent (irregular gaps between windings etc.) But still, amazing! Just subsribed your channel!
@M0UAW_IO83
@M0UAW_IO83 4 жыл бұрын
Nice machine, I'd suggest the upright supports would be more stable if the shafts weren't so flexible, also replace the 12V motor with a second stepper
@Delali
@Delali 2 жыл бұрын
What a thing of beauty. This build is really innovative. I love it. Simple but yet effective. We should collaborate on a build sometime my friend. Cheers!!
@seryj591
@seryj591 8 ай бұрын
Приятно смотреть,смесь человеческого разума с механикой.
@levimadsen5224
@levimadsen5224 3 жыл бұрын
Before cutting the wheel, you should plane it so that it's absolutely flat. Could help reduce the wobble.
@anilverma352
@anilverma352 3 жыл бұрын
बहुत सुन्दर एक कम रूपयों में अच्छी मशीन और वर्किंग भी अच्छी पूरी मेहनत से बनी है काम भी अच्छा करेगी थैंक्यू
@mmaranta785
@mmaranta785 3 жыл бұрын
I remember using a coil winding machine with #46 AWG magnet wire or something and 3000 turns on a 1 inch diameter toroid for a current sensor.
@MikeHillMusic
@MikeHillMusic 4 жыл бұрын
Had to turn off due to the music. However, I love the project. Truly impressive! But.. please consider ditching the music. 👍🏼
@ziksou4366
@ziksou4366 Ай бұрын
Welcome, my dear brother. I hope you continue making a new machine because what you make is very wonderful
@haraldpettersen3649
@haraldpettersen3649 3 жыл бұрын
A small ingenious machine made of a few pieces of plywood, cheap ball bearings and a few pieces of plastic. Buying such a machine at the store costs more than your car :)
@albertmagician8613
@albertmagician8613 3 жыл бұрын
I guess that adding a wire guide at the supply coil would give a neater result, although it would not much affect the functionality of the induction.
@EmmittBrownBTTF1
@EmmittBrownBTTF1 4 жыл бұрын
Might better to turn your latch around so centrifugal inertia will push it closed, a detent pin would also hold the securely. Wouldn't hurt to put a hinge in the ring, so larger toroids can be inserted.
@s.sradon9782
@s.sradon9782 2 жыл бұрын
replace all wooden parts with plastic or metal, use softer and thicker rubber for plastic rollers & calibrate the machine so the wire being wound onto the core has more tension, some sort of wire guide & tensioner would be useful here.
@ashokballatagi1318
@ashokballatagi1318 4 жыл бұрын
Even after seeing the video we struggle to imagine the concept. God gift. Thanks
@rafaelx.418
@rafaelx.418 3 жыл бұрын
Hello, it is amazing design, thank you and congratulations, I subscribed. One point about use of plywood for precision projects, try using hardwood plywood, it will machine smoother, parts will be more rigid and will keep your winding tolerances lower. Also do not leave precision wooden projects unsealed, hygroscopic expansion of plywood panel in XY dimension is 0.2mm/m for each 1% RH and thickness as much as 1mm/m per 1% RH.
@ag6286
@ag6286 4 жыл бұрын
3d printer would do wonders, also a V-score groove on the wheel and stepper motor for improved accuracy
@jimmyhoffmann4950
@jimmyhoffmann4950 4 жыл бұрын
Better yet stepper motor with planetary gearbox
@ag6286
@ag6286 4 жыл бұрын
@@jimmyhoffmann4950 yeah, that belt setup will allow for a lot of slip potentially with thicker gauge wire
@montyhoutchens9217
@montyhoutchens9217 3 жыл бұрын
@@jimmyhoffmann4950 6⁶
@fddecorationjepara6057
@fddecorationjepara6057 3 жыл бұрын
Nggeh Nggeeh saestu wreeeeeeeeeeereeee New Neweeeeeeeeee eeeeeeeeeee e eNewweeesee weedok wesee3a
@jimmyhoffmann4950
@jimmyhoffmann4950 3 жыл бұрын
@@fddecorationjepara6057 good point
@ma-lakshmifabricator7549
@ma-lakshmifabricator7549 9 ай бұрын
Overall, this is a highly informative and enjoyable video for anyone interested in engineering. It showcases your talent and expertise while providing valuable insights and inspiration to fellow enthusiasts. Keep up the great work, and I look forward to watching more of your content in the future 👍👍👍
@invisiblealex007
@invisiblealex007 4 жыл бұрын
that's incredible and finally useful device on Arduino)))) and it is not a toy. Great job and tech idea
@electronic7979
@electronic7979 4 жыл бұрын
An excellent video. I watched every second with pleasure.
@MrInnovative
@MrInnovative 4 жыл бұрын
Thank you very much!
@enki_220
@enki_220 4 жыл бұрын
kzfaq.info/get/bejne/r5Z5l62mqZnLl58.html
@gyrogearloose1345
@gyrogearloose1345 8 ай бұрын
This is very cool. Quite amazing! I'm sure with this prototype running you can see where and how to refine it. Nice work Mr Innovative, keep on going!
@jpjp8964
@jpjp8964 4 жыл бұрын
Wonderful projects, building quality is superb, congratulations sir
@DerrickJolicoeur
@DerrickJolicoeur 3 жыл бұрын
Looks like it could benefit from something to align the wire coming off the spool to make the winding more consistent, but this is a great idea none the less
@grzegorzszymanowski4091
@grzegorzszymanowski4091 4 жыл бұрын
Hi, great work! I was do similar machine for standard transformers many years ago (over 30). Speed of my machine was lower to more control of the layering.
@fgbhrl4907
@fgbhrl4907 4 жыл бұрын
Very cool. However, that wandering bandsaw.... Maybe the next project should be making some guides for it? Also, it would be cool to be able to wind much smaller toroids -- like 1" diameter or less. I think that would be difficult though.
@jimboyfederigan6598
@jimboyfederigan6598 3 жыл бұрын
To the owner of this channel thanks this is the type of machine i was invisioning in my dreams thanks for making this happen
@big_o1952
@big_o1952 3 жыл бұрын
One question why isn't this a product
@joeabad5908
@joeabad5908 Ай бұрын
A very nicely built project.. my hat is off to you, Sir!!
@vladv8434
@vladv8434 4 жыл бұрын
Больно смотреть сколько мучений без 3D принтера.
@serzgregory9124
@serzgregory9124 3 жыл бұрын
А откуда взялся желтенький боксик? Не из-под 3D?
@kevinbyrne4538
@kevinbyrne4538 4 жыл бұрын
VERY impressive ! This project must have required Much time and effort. Congratulations.
@Todestelzer
@Todestelzer 4 жыл бұрын
Nice work. Consider buying a 3d Printer as well.
@NickDe39
@NickDe39 3 жыл бұрын
Numbers were considered magical or mysterious, numbers with the most primes were consider special like 60 seconds in a minute, 60 minutes in an hour etc. It Tesla selected 120 Hz instead of 60, our motors and transformers would be one quarter the size. But with solid state rectifiers converting AC to DC and pulsing a toroid core say at a million hertz wall wart chargers could be made extremely small as well as any AC to DC power supply. I never wound toroid cores, left that job to someone else, just designed them. Were called switchmode power supplies.
@victoryfirst2878
@victoryfirst2878 3 жыл бұрын
YOu are hands down on clever person. Really enjoyed the show.
@td_44
@td_44 4 жыл бұрын
Натяжение долно регулироватся иначе провод будет болтатся на трансформаторе, или ездить по магнитопроводу.
@Joe_Maputo
@Joe_Maputo 4 жыл бұрын
Тоже заметил такой недочет. Вроде автомат, а витки укладываются хуже ручной намотки. Еще и шаг намотки гуляет 00:37
@vvvladimirrrk
@vvvladimirrrk 4 жыл бұрын
@@Joe_Maputo Цепляетесь к мелочам, пять минут доработать напильником :), Молодец чувак, хорошая машинка !
@ikhbinikhbin7473
@ikhbinikhbin7473 4 жыл бұрын
@@vvvladimirrrk "ДЬЯВОЛ КРОЕТСЯ В МЕЛОЧАХ" вот надо было СНАЧАЛА напильником доработать, а потом уж и хвастаться. угу.
@samuel_towle
@samuel_towle 4 жыл бұрын
I agree that your toroidal coil winding machine makes for a good demonstration. However, unless you are making production runs, I would have to question the practicality of the build. I doubt there is enough tension to wind wire thicker than 22 to 24 gauge. Given the size of the shuttle and ring, small internal diameter cores are out of the question. You could reduce the size of the ring and shuttle by using the ring as wire storage and reversing the ring to load wire onto it. A metal ring could reduce size further, but also be harder to drive. Back in the late 1980's I wound and tested prototype coils and transformers. One of the designs required 500 turns of 40 gauge wire on a torroid about 20 mm O.D. I used a 6" wooden handle for a Q-tip with a notch at each end as a wire shuttle. Winding 5 of these units took about 2.5 hours.
@MrInnovative
@MrInnovative 4 жыл бұрын
smaller toriod possibility will be consider in next upgrade.
@ivancho5854
@ivancho5854 Жыл бұрын
Using the ring itself for wire storage is interesting, though the ring would have to be mechanically more complex. Also a correction to the software may be required depending on the design. All the best.
@davidcerva9864
@davidcerva9864 3 жыл бұрын
That was surprisingly satisfying to watch. Great job :)
@johnnybadea
@johnnybadea 3 жыл бұрын
There is a major flaw in your project. The rollers that keep toroid in place are fixed. They have to be self-adjustable when you have to fil the toroid with more wire so it becomes bigger in diameter. Also you would be able to fit a bigger toroid, which you can't do now... Otherwise nice project!
@user-is1ie5zk2z
@user-is1ie5zk2z 3 жыл бұрын
Отличное видео и идея, отличный токарный станок для реализации небольших задач! Спасибо
@jamest.5001
@jamest.5001 4 ай бұрын
It eould be s good addition to getba few small endmills you can put in the drill. To do plunge cuts in metal, and slow gentile side cuts in woods and plastics Maybe some small cuts in aluminum a 1/4" - 6mm and maybe 12mm- 1/2" and some in-between. Possibly make adapters to allow larger end mills to be used. Maybe an adapter that allows a 3"-4" lathe chuck to fit a drill, then end Mills will fit, and many other things , if you ho that far, just as well build a tilt lathe /mill. A lathe that can double as a mill. It would be small but handy. Allow work about 3"x12" roughly possibly 6" x12" tibe milled s cross slide and mill vise, about anything could be built then, (id use it to build a larger lathe/mill 😜 6"-8" chuck,36" travel/bed)
@RDTOYS
@RDTOYS 4 жыл бұрын
Literally Brother You are Inventor .., I was seen your many Efforts for This Project.
@crankhandle
@crankhandle Жыл бұрын
Well done, impressive work making complex parts by hand! Imagine this guy let lose with a 3d printer
@douffinguessan1129
@douffinguessan1129 Жыл бұрын
Très belle initiative je vous remercie c'est Vraiment merveilleux.
@SteveCircuits
@SteveCircuits Жыл бұрын
Nicely done! Something that could be useful: Forward and Reverse! If you add a guide to help improve the wire positioning, this could let the user fine tune the position accuracy by winding or unwinding till it's just right.
@shyleshsrinivasan5092
@shyleshsrinivasan5092 4 жыл бұрын
Thanks for sharing this build ! Well made !
@likewisepro
@likewisepro 3 жыл бұрын
Mr Innovative, is the user capable of introducing the desired inductance? Input parameters would be toroid diameters, wire copper size. Then the system would compute the needed turns. Just an idea.
@KimMoth
@KimMoth 3 жыл бұрын
I bet the uneven windings are mostly down to the fact the wire doesn't go through a guide after coming off the spool. The way the windings are bunched and spaced in a sort of repeating pattern probably reflects the angle the spool gave it as it unwound.
@AltGrendel
@AltGrendel 4 жыл бұрын
Much better with the sound off. Fascinating project, looks great.
@oliverdobson5199
@oliverdobson5199 4 жыл бұрын
Excellent! As for improvements maybe make the ring opening larger (to add and remove large toroid coils more easily) - I’d have 2 splits rather than the 1 you have. Also your code can adjust for toroid diameter but can the machine? Maybe need to add adjustment in the 3 supports in/out. Also is your code adjusting for diameter increase of multiple winding layers? Does it auto stop of out of wire? Can the wire diameter be changed?
@martinmengh
@martinmengh 4 жыл бұрын
nice lathe. I've got one too. It's the first time I've seen the wood working attachment actually used on this lathe.
@klave8511
@klave8511 4 жыл бұрын
You can be proud of this achievement! Well done, except for the flashing LED which looks like a big fat electrical spark to me and had me backing away from my screen 😉
@MrInnovative
@MrInnovative 4 жыл бұрын
I have burned that sensor off camera so I changed the smd IC meanwhile unfortunately LED trace also get removed so I added external LED to it..
@The_Unobtainium
@The_Unobtainium Жыл бұрын
I heard as well that painted plywoods magnetic permeability and its saturation point is much higher than the one you can find in usual ferrite cores:D
@marcelonepomuceno3930
@marcelonepomuceno3930 4 жыл бұрын
SENSACIONAL MEU AMIGO! PARABENS!
@user-bg5ot2hw9m
@user-bg5ot2hw9m 3 жыл бұрын
Отлично! Спасибо за идеи! Хороший станочек! Прекрасная работа,золотые руки!
@gyggit
@gyggit 3 жыл бұрын
вирус не поймал по его первой ссылке?
@cristianilie8857
@cristianilie8857 3 жыл бұрын
Great engineering work! Thanks for sharing this with us! Will start to buil it soon! Thanks again
@Reno_Slim
@Reno_Slim 4 жыл бұрын
I had to hand wind torridial transformers for proprietary power supplies. A machine to help out would have been nice.
@oneilgoisot9615
@oneilgoisot9615 4 жыл бұрын
Replace your IR sensor by a hall effect sensor and magnet it will solve all your problems
@nixxonnor
@nixxonnor 4 жыл бұрын
Why? Either method count every completed revolution
@markrichards5630
@markrichards5630 4 жыл бұрын
Both are speed of light things so timing should be the same. But with light you have the option to narrow the beam or use a slit or lens to really hone in on when you want the count to increment. With a magnet and hall effect its harder to get around the magnetic field rising over time as the magnet approaches. The waveform is always sinusoidal for a mag/hall combo (and you have to pick the threshold value off that hump), but could be closer to square wave with a slitted or lensed led. But we're really splitting hairs here. At this "low" frequency you could dial either in for equally good results.
@oneilgoisot9615
@oneilgoisot9615 4 жыл бұрын
@@nixxonnor it's maybe an illusion but in the video we don't see the blink at every revolution so I think the ir sensor isn't aligned with the black tape
@oneilgoisot9615
@oneilgoisot9615 4 жыл бұрын
@@markrichards5630 I'm agree with you for the question of frequency but with a hall effect sensor you don't really need to be aligned with the magnet so it's easier to count it's the only reason to choose this sensor
@nixxonnor
@nixxonnor 4 жыл бұрын
@@oneilgoisot9615 Actually I think the missing LED blinks is a camera shutter speed issue as the LED only lights up for a very short moment.
@BarioIDL
@BarioIDL Жыл бұрын
you can use 3 window rollers, take out the rubber ring from 2 of them
@valshaev1145
@valshaev1145 4 жыл бұрын
Despite some misspelled words, the machine looks as a professonal grade, not production, but professonal! For how much you would sell it for? Like!
@TechBuild
@TechBuild 4 жыл бұрын
Suggestion: Replace the 16x2 LCD screen and the rotary encoder with a touchscreen TFT display. It can help speed up the process of setting up the parameters.
@scharkalvin
@scharkalvin 4 жыл бұрын
This is a nice design if you need to wind toroidal transformers using a large core. It isn't suitable for winding small RF toroids that have cores under an inch in diameter. There are machines that have an internal bobbin inside of the shuttle. These need to be power wound before being unwound when winding the core.
@skaterdudeabides
@skaterdudeabides 4 жыл бұрын
Damn. Such clean work. I learned a few things. :)
@kingmasterlord
@kingmasterlord 4 жыл бұрын
I see several improvements I can make for example a guide arm for the wire(more even spacing and all that), definitely going to print one of these when I get a 3d printer
@edilbertomendoza5359
@edilbertomendoza5359 4 жыл бұрын
Good job! Getting stability or robust is only a little step. Congratulations. You gave me a lot of ideas. Really you did.
@zachx4338
@zachx4338 4 жыл бұрын
I feel like adding more indicators, maybe 2 or 4 rather than 1 would help make things more precise. Instead of 1 step per rev, do half or quarter steps, in relation to the amount of indicators.
@PeteVanDemark
@PeteVanDemark Жыл бұрын
You made a beautiful thing. Very nicely done!
@Kayram1
@Kayram1 4 жыл бұрын
Awesome build. Appreciate your effort. Lot of effort must have be put to make this. 👍👍 If you were to rebuild what changes would you make ? As I would like to build one like this.
@ganeshpavan1892
@ganeshpavan1892 4 жыл бұрын
Ur the first person to make this machine I mean diy project
@alejandrodelabarra2838
@alejandrodelabarra2838 4 жыл бұрын
Muy bueno!! Todo de madera y con rodamientos, como me gusta a mí. Un espectáculo. Thanks for sharing your knowledge wiith us!!!!!
@redportleft
@redportleft 3 жыл бұрын
I much prefer videos where they show the project working and then how they made it.
@acestudioscouk-Ace-G0ACE
@acestudioscouk-Ace-G0ACE 3 жыл бұрын
Congrats on the project ...but lose THAT MUSIC!
@andreykrasehin2823
@andreykrasehin2823 3 жыл бұрын
особенно мне *понравилась* пайка проводов к электромотору
@TechBuild
@TechBuild 4 жыл бұрын
Great to see something new. Keep making such projects and all the best!
@Demurin
@Demurin 4 жыл бұрын
Идея хорошая, но вот плотность укладки и шаг слишком растянутый и не ровный. Ещё бы неплохо добавить автоматический расчет длины намоточного провода с учетом толщины и требуемые первичные и вторичные обмотки для трансформаторов и генри для индуктивностей.
@davey2k12
@davey2k12 4 жыл бұрын
That's spot on lol Need to make smaller one cud be bobbin type and moves coil out the way be harder to make tho ...that needs a number pad with +100 button lol
@ITpanda
@ITpanda 3 жыл бұрын
A means of pausing system on wire running out would be nice. So your not guessing on wether or not you have enough for project or so you could finish wire on spool and attach additional so to avoid additional waste.
@phab2protango374
@phab2protango374 4 жыл бұрын
You need lots of improvement 1 the copper wire spoller should have a metal polished hole through which the wire unwinds Will give more even turns Take time out and see a stitching machine , how it's Spool opens up n down but the end portion of thread goes linear 2 Also a little tension on the wire , again like a sewing machine has even tension 3 Your wooden wheel is a bit wobbly, also if it is not balanced like a car/bike wheel it can introduce vibrations at high speeds But excellent work never the less A 3d printer to make parts will go a long way , though not necessary , as you yourself have shown.
@ashokballatagi1318
@ashokballatagi1318 3 жыл бұрын
Great engineering job. Not all can not do. Only high knowledge person can do. Thanks for edua
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