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Dad filmed Emergency Landing after Engine Failure | Diamond DA40 NG

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Prop Clear

Prop Clear

Күн бұрын

Пікірлер: 171
@lawrencemartin1113
@lawrencemartin1113 Жыл бұрын
Fantastic work! Glad that all ended so successfully and, not only was no one hurt, but that aircraft looks to be in really great shape after a forced landing! (Apart, of course, from the engine!). What I want to know is, what was the 'BANG!' you heard and why did the engine fail?
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@lawrencemartin1113
@lawrencemartin1113 Жыл бұрын
@@PropClear Thanks! Good to know the reason. Glad it ended so successfully for all involved in the aircraft.
@semiprofessional8470
@semiprofessional8470 Жыл бұрын
​@@PropClear wow such a small item brought the plane down. I'll stick to dinosaur engines that will run missing an entire cylinder
@gsilva220
@gsilva220 Жыл бұрын
The report says the injector #3 had been removed at a prior date due to a leak. During the incident, the injector was somehow shot out of the cylinder head (explaining the loud bang) and the high pressure line also came loose, causing the loss of fuel pressure to the other injectors.
@gsilva220
@gsilva220 Жыл бұрын
@naborsimbor5752 If it were a piper, and somehow one of the spark plugs were shot out of the cylinder head, the engine would keep running on 3 cylinders.
@user-rg7ye3ni5f
@user-rg7ye3ni5f Жыл бұрын
As a flight instructor with some 1500 hours on the DA40, i find it remarkable that you would be able to complete all these items with an engine failure below 1000ft. I'm not sure even I would have had the resources' to pull up and complete two independent checklists, brief ATC, PAX as well as secure the engine before touch down, all within around 60 - 90 seconds. I would probably have done a simplified troubleshoot fast by memory and then focused on setting up a solid final to land. Just some reflections, very well done to you! I did also once have a "partial" engine failure on the DA40NG, with it only producing some 35% load over mountains, yet they are very reliable, would take the E4 over a Lycoming any day.
@industrieundtechnik1761
@industrieundtechnik1761 Жыл бұрын
Yes I see very reliable this plastic trash ton with many death people due to the cdi mercedes a class engine first converted by thielert germany. I prefer a lycoming any day in front of this garbage. I need to say this engines had already many problems in the a class. The injectors easily burn holes in the pistons if there is a little problem.
@rodsilva80
@rodsilva80 Жыл бұрын
@@industrieundtechnik1761 you must be fun at parties
@planespeaking
@planespeaking 4 ай бұрын
​@@industrieundtechnik1761This is a very safe aircraft and one of few that actually have a safety cell on event of a crash. The engine is reliable and safe. You have zero facts to back up your assertions
@manitouproject
@manitouproject Жыл бұрын
Nicely done 👍 I was on the frequency that day somewhere in the region of Brienz on the way back to LSZI from a flight in the alps and still remember the mayday calls, the ZRH Information controller saying "Emergency in progress, stand by" to other pilots and then reports of the save landing from another plane circling above 😉 The other pilot reported no significant damage to the aircraft and was counting the people climbing out of the aircraft. The controller then compared it to the number of people on the flight plan, so make sure these numbers are right and/or report any change when on frequency after takeoff.
@PropClear
@PropClear Жыл бұрын
wow thanks for sharing your story of that day. Must have been an uneasy felling hearing that someone else has en emergency and a lot of relief hearing that everything went fine. Hope you had a good flight that day anyways!
@flomoose7315
@flomoose7315 Жыл бұрын
Wow. Great reaction. I doubt that many would’ve reacted the same way you did! Excellent job, flying, navigating, end EVEN communicating👍🏼. Be proud and humble on what you’ve experienced
@mikegiangreco6216
@mikegiangreco6216 Жыл бұрын
Wow, so calm and relaxed with 22 years old! You did a great job - congrats- and thank you for explanation. Emergency checklist ist what I should go through 😅✌🏽
@PropClear
@PropClear Жыл бұрын
Great takeaway, I think we would all benefit from going through the emergency checklist more often :)
@PureGlide
@PureGlide Жыл бұрын
Glider pilot here, I've done about 85 paddock landings so far. My thoughts: - Great paddock selection! It's something we train for, but most pilots wouldn't. Choosing a good field, that's flat, big enough, and not downhill or too downwind is the most critical thing. - Most dirt paddocks like that tend to stop pretty quickly. Longer grass fields tend to stop much more quickly than an airfield too. - Anywhere under 1000 feet, I would focus heavily on choosing a good field and focusing on the circuit and landing. Anything else (e.g. radio, engine failure checklists) is distracting from the critical thing which is flying the plane. Of course try the obvious things, and if you're high enough then do them all. - The circuit is the way glider pilots give themselves options. Straight in, if you hit heavy sink there's nothing you can do. If you're on downwind or base you can turn in sooner depending how fast the descent is. Great job, couldn't have gone better :)
@bernieschiff5919
@bernieschiff5919 Жыл бұрын
What also helped here is the good design of the Diamond nose wheel assembly, a sturdy steel arm swept back at a sharp angle, minimizing the tendency to dig in into soft ground and flip the airplane. Also, a good soft field landing by the pilot.
@ceansilorcaso5820
@ceansilorcaso5820 Жыл бұрын
The DA40 is also design to have good gliding qualities better than other personal planes. I think, that make a big difference.
@mahavishnus9191
@mahavishnus9191 Жыл бұрын
We feel the real pilot in us when we attempt such emergencies.
@gsilva220
@gsilva220 Жыл бұрын
The report says the injector #3 had been removed at a prior date due to a leak. During the incident, the injector was somehow shot out of the cylinder head (explaining the loud bang) and the high pressure line also came loose, causing the loss of fuel pressure to the other injectors.
@boikostanislav7962
@boikostanislav7962 Жыл бұрын
Bravo !!! Très bien géré. Et merci pour le retour d’expérience ! C’est incroyable!
@dermick
@dermick Жыл бұрын
Great flying and managing this emergency! I hope you continue to fly and have a long and rewarding career as an ATP. Happy to have a great pilots like you up front when I fly commercial.
@PropClear
@PropClear Жыл бұрын
Much appreciated!
@harborhoffer
@harborhoffer Жыл бұрын
Fantastic video and an excellent recount of this pilot's emergency landing. Thank you for sharing this textbook happy ending.
@99kevin99
@99kevin99 Жыл бұрын
Nice presentation. You made your flight instructor VERY PROUD that day! KP
@N807DS
@N807DS Жыл бұрын
Congratulations from a felliw ex DA40 pilot. well done
@archer494
@archer494 11 күн бұрын
Danke für Dein Video. Hoffe mir bleibt nie der Quirl stehen, aber wenn dann hoffe ich daß ich das auch so cool hinkriege wie Du anscheinend. Notlandeübung kann man so oft machen wie man will. Ist einfach nicht das Gleiche. Wie hoch AGL warst Du als der Motor ausfiel? Schaut nach 3000+ aus.
@skipgetelman3418
@skipgetelman3418 Жыл бұрын
Amazing job by this young pilot
@aroopghosh1381
@aroopghosh1381 Жыл бұрын
Superb performance
@fulviosanna
@fulviosanna Жыл бұрын
Good job and right attitude from the pilot, congrats! I was wondering what the problem was with the engine and what caused the engine failure, thanks!
@PropClear
@PropClear Жыл бұрын
it's written in the pinned comment answer
@Archonch
@Archonch Жыл бұрын
Wow congrats
@SirBender
@SirBender Жыл бұрын
Hut ab! Tolle Leistung 🙋🏻‍♂️
@lucmatter9601
@lucmatter9601 Жыл бұрын
You will also land that ATP-job, no doubt. Congrats
@languystephane
@languystephane 4 ай бұрын
Amazing story, amazing outcome
@garyandthebat
@garyandthebat Жыл бұрын
Well done mate.
@ericwilson8000
@ericwilson8000 Жыл бұрын
Excellent landing Sir!
@StanwoodStudios
@StanwoodStudios Жыл бұрын
Great video, bravo to the pilot! Nice work!
@JulienGordon
@JulienGordon 9 ай бұрын
Great video!! Thanks for sharing
@DownhilllRacer
@DownhilllRacer Жыл бұрын
Congrats! As an emergency landing can just be trained in theory as long as you not need it, I am pretty sure he managed that well because his trainingg wasn't that long ago. I think even more experienced pilots will not manage that well.
@piper0428
@piper0428 Жыл бұрын
Awesome!
@SteenPedersen
@SteenPedersen Жыл бұрын
Great job. I hope I can stay that calm if it every happens to me. Would have been interesting to hear, what went wrong with the engine?
@PropClear
@PropClear Жыл бұрын
read pinned comment & answer
@stevewinegar6364
@stevewinegar6364 Жыл бұрын
Amazing execution. I won’t fly again until I am that fluid in my procedures. I could have gotten down into a field if available, but I wouldn’t have remembered my proper restart procedures, fuel check, ECU check, fuel shutoff, master shutoff, etc. I need to get more rigorous. Thanks for showing us what “right” looks like! What engine was this aircraft equipped with? I assume the diesel due to the ECU switch.
@PropClear
@PropClear Жыл бұрын
It is equiped with an Austro Engine E4-A (Diesel) - former Mercedes A-Class car engine
@SwissFlightInsight
@SwissFlightInsight Жыл бұрын
amazing video thanks
@lukemurphy7726
@lukemurphy7726 Жыл бұрын
I flight instructed in the DA40NG for 350 hours. The engine reduced power to 72% on me while taking off. It happened departing a short runway in the mountains (KGWS). It happened at rotation speed and there was not enough runway to abort. I had to take the problem in to the air and I barely cleared the trees. The turbocharger wastegate controler was to blame. I don’t trust the Austro engine and I won’t fly the DA40NG anymore.
@TzarbombahMusic
@TzarbombahMusic 11 ай бұрын
they're garbage aircraft
@brianbradley8244
@brianbradley8244 11 ай бұрын
Why did it fail?
@LSZH_aviation
@LSZH_aviation Жыл бұрын
R.I.P HB-SGU 😭
@PropClear
@PropClear Жыл бұрын
HB-SGV, but she is back in the air
@LSZH_aviation
@LSZH_aviation Жыл бұрын
@@PropClear no no i mean from a few weeks ago HB-SGU Crash in the approach
@thepenmen22
@thepenmen22 Жыл бұрын
He had to stay there for 8 hours after the landing??? That's insane!!!!!
@FryChicken
@FryChicken Жыл бұрын
Swiss bureaucracy
@spitfireinvasion
@spitfireinvasion Жыл бұрын
Can you elaborate why an off field landing is preferable in brown fields as opposed to green or planted ones? My first reaction would have been to avoid brown fields, my fear is to get the nose wheel stuck and flip the plane in a muddy, brown field…
@qwequ777
@qwequ777 Жыл бұрын
Just guessing - maybe it is because it is hard to judge the amount and type of growth. From 1000ft everything looks like grass. You go down and realize at 60ft that it's 6ft tall corn with grown cobs. Brown means earth, guaranteed. Also even if it is grass, that is probably more slippery than soil. Aviation experts, please clarify!
@englishclive
@englishclive Жыл бұрын
@@qwequ777 In the UK we have lots of fields, TBH I've not thought about colour and my first reaction to 'brown fields' was they would usually have just been ploughed or tilled in someway and so wouldn't be my first choice. Green ones would be my preference if I had to flip a coin though stubble is brown and good. I suppose in mountainous places green fields would generally be rather undulating and only farmed fields are definitely flat. No expert here obviously....
@possel4747
@possel4747 Жыл бұрын
I am always looking for the green-ish fields with a brown or yellow tinge. These are the ones with shorter grass (and possibly sheep!). Lush green is liable to be long (unseen until too late) and rich brown implies freshly ploughed (bad) or harrowed (possiblly good). I was disappointed there was not more in the film about the choice of field whilst airborne, regarding the wind direction and strength, plus avoiding people and wires.
@650tonyd
@650tonyd 5 ай бұрын
This my friends is why Cirrus has a parachute
@jhonk.m.k.6441
@jhonk.m.k.6441 Жыл бұрын
Well done! Why do have to shut the engine and fuselage in such a case off and why you should land on brown areas?
@PropClear
@PropClear Жыл бұрын
Green fields look all the same from above but some of them could be covered with 2m high corn or other plants. brown you always know what will await you. also better for firefighter and ambulance to find you
@jstflyin
@jstflyin Жыл бұрын
Exemplary dead stick landing by the pilot, well done. The video is a bit superficial. What was the technical reason for the engine failure?
@PropClear
@PropClear Жыл бұрын
Thanks for your feedback. To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@SimonAmazingClarke
@SimonAmazingClarke Жыл бұрын
Well done. What was the issue with the engine.
@PropClear
@PropClear Жыл бұрын
Well done indeed! To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@MGA19a
@MGA19a Жыл бұрын
Well this is a kinda pilot you wanna have in your airliner as well !
@d-X-es4vi
@d-X-es4vi Жыл бұрын
What happened to the engine ? 🇨🇵✌️
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@d-X-es4vi
@d-X-es4vi Жыл бұрын
@@PropClear thanks!
@chicobicalho5621
@chicobicalho5621 8 ай бұрын
Missing from this post is the most important question: What was the reason for the engine failure?
@beomsukim3929
@beomsukim3929 Ай бұрын
So what happened to the engine?
@everflywings
@everflywings Жыл бұрын
Excellent job. What went wrong with the engine please?
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@everflywings
@everflywings Жыл бұрын
Thank you! Human error again! I own a Bonanza F33A and fly alot. What scares me most is human error, especially after the annual inspection
@britfisher3372
@britfisher3372 9 ай бұрын
Anyone have a comment how a Cirrus would do on this? Too low for the parachute, I’m wondering if the glide characteristics of the DA 40 helped them to survive?
@philipohmes9395
@philipohmes9395 Жыл бұрын
I was curious enough to want to read the Final Report as to the cause of the engine failure. Some mechanic did not install the proper fittings on the fuel line for piston 3 during a repair procedure on the engine. This caused a fuel line failure as the fuel line decoupled from the engine and thereby causing loss of fuel to the engine, rather quickly. Just wondering if a Pilot should during the pre-flight check, now look at the engine, to see of all of the lines are in proper working order? The failure is quite noticeable from the picture taken from the investigation.
@PropClear
@PropClear Жыл бұрын
there is no way to see such a failure in a pre flight check. This his hidden behind many coverings. In the picture it looks noticeable, because the engine was fully open.
@maxagent86
@maxagent86 Жыл бұрын
What was the cause of the engine failure? What engine?This could have been added to the video. Thank you for sharing.
@PropClear
@PropClear Жыл бұрын
Final report from the Swiss Aviation Council: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@tonyreid833
@tonyreid833 Жыл бұрын
Yes brilliant result But what failed on the aircraft please ?
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@alexknizhnik5686
@alexknizhnik5686 Жыл бұрын
Nice job! So what was the engine failure reason?
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@archevoked6468
@archevoked6468 8 ай бұрын
But...for godsake, what happened??? Why the engine got off??? 🤦🏻‍♂️🤦🏻‍♂️🤦🏻‍♂️
@PropClear
@PropClear 8 ай бұрын
check pinned comment
@davegeorge7094
@davegeorge7094 Жыл бұрын
What's was wrong with the engine?????
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@luizroberto844
@luizroberto844 10 ай бұрын
Se tivesse um motor auxiliar elétrico no bordo de fuga da asa, qualquer falha no motor, não ofeteceria risco.
@Sqwr
@Sqwr Жыл бұрын
What failed ?! Great story but we want to know what part of the engine died !
@PropClear
@PropClear Жыл бұрын
Check out the pinned comment from Lawrence Martin with our reply
@arnaudnicolau2093
@arnaudnicolau2093 Жыл бұрын
sooo what cause the engine to fail?
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@englishclive
@englishclive Жыл бұрын
@@PropClear maybe you should put this isn the main description...😉
@wesleyevans8368
@wesleyevans8368 Жыл бұрын
Can we get a update on what caused the engine failure? Diagnosis
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@llg.208
@llg.208 Жыл бұрын
This guy is cool as a cucumber 😎 What was the reason behind the engine failure?
@PropClear
@PropClear Жыл бұрын
Very cool indeed! To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@llg.208
@llg.208 Жыл бұрын
@@PropClear thanks for sharing!
@line-uppilot1038
@line-uppilot1038 Жыл бұрын
woow - we all hope this never happens to us and nobody knows how he will react. nice job dominic
@TheSlickpt
@TheSlickpt Жыл бұрын
Awesome job . What happend to the engine? I cannot read the report.
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@TheSlickpt
@TheSlickpt Жыл бұрын
@Prop Clear thank you very much . Unfortunately only understand English. I really appreciate your help 🙏
@conradsenior5843
@conradsenior5843 Жыл бұрын
what was the problem with the motor?
@PropClear
@PropClear Жыл бұрын
check the pinned comment
@dimsler7934
@dimsler7934 Жыл бұрын
What was the cause of the engine failure? this aircraft is the CD135 version?
@PropClear
@PropClear Жыл бұрын
Austro Engine AE 300 turbocharged common-rail injected 2.0 liter diesel engine with 168 hp and EECU single lever control system. All details here: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@berndl
@berndl Жыл бұрын
But why no word about the technical malfunction? What was the reason for the engine failure??
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@NikosWings
@NikosWings Жыл бұрын
Great work and you are lucky you found a good field and flew the airplane properly. But it could had been much worst if things were not perfect. That's why I fly a Cirrus, you pull the chute!
@paularchard5796
@paularchard5796 5 ай бұрын
Does the chute wo4k at 1,000 ft.?
@waynebayley1569
@waynebayley1569 Жыл бұрын
What caused the engine to fail?
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@masonprov
@masonprov Жыл бұрын
What was the problem with the plane?
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@nunyabidness3075
@nunyabidness3075 9 ай бұрын
Why does this plane have the MPP windscreen?
@PropClear
@PropClear 8 ай бұрын
Increased headroom for larger pilots.
@nunyabidness3075
@nunyabidness3075 8 ай бұрын
@@PropClear Cool, thanks.
@tonyreid833
@tonyreid833 Жыл бұрын
But what caused the failure ?
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@westonbadke5434
@westonbadke5434 Жыл бұрын
Was it a blown piston?
@PropClear
@PropClear Жыл бұрын
the fuel injector fall out of the engine block.
@alessandromarino3937
@alessandromarino3937 Жыл бұрын
Was it the austro engine?
@PropClear
@PropClear Жыл бұрын
Yes
@Tundraalex
@Tundraalex Жыл бұрын
I was hoping they were going to tell us what happened to the engine that caused it to fail…
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@dalesiemens
@dalesiemens Жыл бұрын
What was wrong with the engine?
@JSFGuy
@JSFGuy Жыл бұрын
Browse the comment section it's posted several times. Loose fuel connection.
@tomarmstrong1281
@tomarmstrong1281 Жыл бұрын
This is not uncommon for the DA 40. Would have been good to know it there was a specific cause. Engines do not stop for no reason.
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@tomarmstrong1281
@tomarmstrong1281 Жыл бұрын
@@PropClear Thank you for the reply. It might be a case of give a dog a bad name. I was employed by an FTO as CFI / DPE. The school had operated PA 28's for years with very few maintenance issues. It passed into new ownership, and was re equipped with Diamond Aircraft across the fleet. We then had a spate of engines failures on the DA 20's.
@guenthermichaels5303
@guenthermichaels5303 10 ай бұрын
You didn't ask, what was the cause of the engine failure?
@PropClear
@PropClear 10 ай бұрын
read the pinned comment
@guenthermichaels5303
@guenthermichaels5303 10 ай бұрын
​@@PropClearok, sorry. Diesel engine? That's a freak kind of accident. Was this a new plane under warranty? If this had happened in US, there'd be lawsuits pending.
@roger111ify
@roger111ify Жыл бұрын
What cause the engine failure?
@PropClear
@PropClear Жыл бұрын
you can find in the pinned comment
@roger111ify
@roger111ify Жыл бұрын
@@PropClear thank you
@rtenharmsen8424
@rtenharmsen8424 Жыл бұрын
What was the cause???
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@arturo468
@arturo468 Жыл бұрын
AT 00:56 he has trousers on, 2 seconds later he's sitting in shorts - what's all that about?
@PropClear
@PropClear Жыл бұрын
not really Arthur - I only can see the upper body on 00:56. I can fully confirm, that he carried shorts the whole shooting 🙂
@jhonk.m.k.6441
@jhonk.m.k.6441 Жыл бұрын
What scares me even more than an engine failure is a failure of the navigation systems like the rudders. Is there any possibility that this could happen? Fortunately I never saw such a failure.
@PropClear
@PropClear Жыл бұрын
if you stay in the limits of the aircraft, this is very rarely. What's more, you alsways test them on ground before take-off.
@FryChicken
@FryChicken Жыл бұрын
Yeah but why did the engine fail?
@PropClear
@PropClear Жыл бұрын
one of the fuel injector has fallen out. This caused an immediate pressure lost in the common rail system. There was no way to restart an engine without pressure in the rail
@FryChicken
@FryChicken Жыл бұрын
@@PropClear That's terrifying. How did the fuel injector fall out?
@PropClear
@PropClear Жыл бұрын
He was not fited correctly during the last inspection (the last Maintenance was done from the company which the flightschool bought the aircraft) So MFGZ is out of the game
@FryChicken
@FryChicken Жыл бұрын
@@PropClear Unglaublich. Sowas darf nicht passieren.
@PropClear
@PropClear Жыл бұрын
@@FryChicken Korrekt. Wie so oft in solchen Fällen. Trotz allen Sicherheitsmassnahmen. Glück gehabt, ist es nochmals gut ausgegangen. Ich habe genau diesen Flieger vor diesem Vorfall in Norwegen abgeholt und bin damit über die Nordsee geflogen. Wäre es dort geschehen, dann.....
@tradingtimes5752
@tradingtimes5752 Жыл бұрын
Should put a toyota engine in the damn thing they wont quit on you
@AmericusMaximus
@AmericusMaximus Жыл бұрын
Pilot trusts a plane that failed him. What was the problem?
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@AmericusMaximus
@AmericusMaximus Жыл бұрын
@@PropClear Appreciate the thoughtful response. Given the nature of the problem, is the young pilot’s continued trust in and loyalty to the airplane justified? Who is responsible for that mishap, who tightens and checks that union nut? How is it unlikely or less likely to happen again?
@PropClear
@PropClear Жыл бұрын
The engine failure is the result of human error in the maintenance. The aircraft was purchased from the flight school in Zurich shortly before the engine failure. The last work on the aircraft was done by the seller.
@AmericusMaximus
@AmericusMaximus Жыл бұрын
@@PropClear Thx again. It stretches credulity for the pilot to affirm his trust in the “beautiful” airplane and the maintenance thereof, if you do the checks, which obviously weren’t done. He fails to mention it, but there was a breakdown in the production a/o maintenance system(s) that, fortunately, for which the pilot training system compensated.
@user-ol1qm9ey7g
@user-ol1qm9ey7g Жыл бұрын
อันนี้ถ้าเห็นด้วยขอจดสิทธิบัตรคุณคิดว่าไปพักเครื่องบินเป็นของจำเป็นไหมถ้าเครื่องยนต์เกิดขัดข้องผมว่ามันเป็นของที่ควรจะโดนสละทิ้งทันทีเพื่อการลงจอดฉุกเฉิน
@TheKetsa
@TheKetsa Жыл бұрын
zero footage of the touchdown ? wtf.
@Mobev1
@Mobev1 Жыл бұрын
All these planes can have a brs and they all should. He wouldnt be alive if he was in ifr or night flying. Our faa should grant a reward for these manufacturers
@stefanmargraf7878
@stefanmargraf7878 Жыл бұрын
Big hole in the story: why did the engine fail? WTF?
@PropClear
@PropClear Жыл бұрын
To cite the analysis of the Swiss Transportation Safety Investigation Board: „The engine failure is due to the fact that the screw connection between the fuel pressure line and the No. 3 injector came loose, causing a sudden drop in pressure in the common rail injection system. The screw connection came loose because the union nut had not been tightened correctly when the injector was installed.“ The full report is available in German: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
@stefanmargraf7878
@stefanmargraf7878 Жыл бұрын
@@PropClear ​ Thank you very much. To me, the reason of failure or crash is very important information. In that case, the loosening or a fail of tightening of a single screw can lead to an engine failure any time. Thats an issue, linked to the common rail technique. Good job by the pilot as well by the plane, by the way.
@raymondservais2673
@raymondservais2673 10 ай бұрын
Bla Bla Bla. No word on what happen to the engine!!! What was the failure cause? Real amateurs, just for show off!
@Jkur2009
@Jkur2009 Жыл бұрын
Not a good look for Diamond.
@PropClear
@PropClear Жыл бұрын
the reason was a human error in the maintenance from the seller of the aircraft. Diamond should not be blamed for that.
@danizweifler6061
@danizweifler6061 Жыл бұрын
wenn Ihr schon so ein Filmchen reinstellen tut...........dann wäre es nett, wenn Ihr auch den SUST-Bericht (= cause of the engine failure) reinstellen würdet...... = prominent das label der MFGZ inkl. maintenance-Halle-Innenseite zu sehen hilft da nix.... MFG
@PropClear
@PropClear Жыл бұрын
Unter Links im Videobeschreib ist dieser bereits verlinkt :) Ansonsten hier noch als shortcut: www.sust.admin.ch/inhalte/AV-berichte/HB-SGV_SumB_D.pdf
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